无填料振冲法加固吹填粉细砂现场试验研究
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摘要
该文基于无填料振冲法加固机理,结合某近海电厂工程试验区吹填粉细砂的地基处理工程实践,对无填料振冲法加固饱和吹填粉细砂地基的适宜性及加固效果进行了现场试验研究。根据地基处理时孔隙水压力监测情况及原位测试结果,对振冲法施工时的留振时间、振冲点间距等问题进行了分析。试验结果表明,无填料振冲法加固饱和吹填粉细砂地基效果良好,为类似地基处理提供了参考依据。
Based on the mechnism of vibroflotation method without additional backfill materials,combined with ground treatment example by hydraulic backfill silty and fine sand at an electric power plant,the suitability and strengthening effect of vibroflotation without additional backfill materials on silty and fine sand is experimentally studied.The vibration time and the distance between two vibration spots are analyzed through the monitoring condition of pore water pressure and result of in-situ test.The test results show that the vibroflotation without additional backfill materials is a good method for strengthening the hydraulic backfill silty and fine sand,and it provides references for similar ground treatment.
引文
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